2019 Ford Escape Cruise Control Problems
3 owner-reported cruise control complaints from NHTSA data
Data sourced from NHTSA public database. For informational purposes only. Always consult a qualified mechanic.
Owner Complaints (3)
The contact owns a 2019 Ford Escape. The contact stated while driving 55 MPH, the vehicle lost motive power and stalled. The contact stated that the vehicle then failed to accelerate above 10 MPH. The accelerator pedal was depressed, but the vehicle failed to respond. The check engine warning light was illuminated. The vehicle was towed to the local dealer, where it was diagnosed that the intake manifold needed to be replaced. The vehicle was repaired. Additionally, the transmission was previously replaced by the same local dealer. The manufacturer was contacted, and the contact was referred to the NHTSA Hotline for assistance. The approximate failure mileage was 88,000.
The contact owns a 2019 Ford Escape. The contact stated that there was smoke coming from the tailpipe. While driving, the vehicle was slow to respond. Additionally, the contact’s son, who is a mechanic, informed her that there was water entering the engine. There were no warning lights illuminated. The vehicle was taken to the local dealer, where it was determined that the vehicle was built with the wrong engine. The mechanic informed the contact that the engine was a long-block engine and should be a short-block engine. The vehicle was not repaired. The manufacturer was contacted, but no assistance was provided. The approximate failure mileage was 75,000. The VIN was not available.
TL* THE CONTACT OWNS A 2019 FORD ESCAPE. THE CONTACT STATED THAT WHILE DRIVING AT LOW SPEEDS, THE VEHICLE SUDDENLY SURGED FORWARD TO THE RIGHT AND CRASHED INTO A UTILITY POLE. NO INJURIES WERE REPORTED. A POLICE REPORT WAS TAKEN AT THE SCENE. THE VEHICLE WAS TOWED TO THE LOCAL DEALER FRIENDLY FORD (2800 N. TELEGRAPH RD, MONROE MI.) THE CAUSE OF THE FAILURE WAS NOT DETERMINED. ALSO, WHILE DRIVING AT VARIOUS SPEEDS AN ABNORMAL NOISE WAS PRESENT COMING FROM THE REAR OF THE VEHICLE. THE NOISE WAS MOST NOTICEABLE WHILE DRIVING DOWN AN INCLINE. THE VEHICLE WAS ALSO TAKEN TO THE DEALER FOR THIS ISSUE HOWEVER, THEY WERE UNABLE TO DUPLICATE THE FAILURE. THE MANUFACTURER WAS NOTIFIED OF THE FAILURES. THE FAILURE MILEAGE WAS 500. *JS