MyCarTSB

2006 Ford Focus Engine Problems

7 owner-reported engine complaints from NHTSA data

7
Complaints
1
Fires
Jan 2015Dec 2008
Date Range

Data sourced from NHTSA public database. For informational purposes only. Always consult a qualified mechanic.

Owner Complaints (7)

mediumENGINE
Filed: Jan 2015

TL* THE CONTACT OWNS A 2006 FORD FOCUS. THE CONTACT STATED THAT WHILE DRIVING AT APPROXIMATELY 50 MPH, THE ACCELERATOR PEDAL FAILED TO RETRACT AFTER BEING DEPRESSED. THE FAILURE OCCURRED ON SEVERAL OCCASIONS. THE VEHICLE WAS TAKEN TO AN INDEPENDENT MECHANIC WHERE IT WAS DIAGNOSED THAT THE THROTTLE BODY NEEDED TO BE REPLACED. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS MADE AWARE OF THE FAILURE. THE FAILURE MILEAGE WAS 100,000.

NHTSA #: 10673021
mediumENGINE AND ENGINE COOLING,POWER TRAIN,AIR BAGS
Filed: Nov 2011

I PURCHASED 2006 FORD FOCUS ZX3 IN MAY OF 2006. IT WAS A BRAND NEW CAR WITH ONLY 8 MILES ON IT. WHEN I PURCHASED THE CAR IT WAS VERY LOUD AND ROUGH. I THOUGHT IT WAS BECAUSE IT WAS NEW AND NEEDED SOME TIME TO BE DRIVEN. AFTER THREE AND HALF YEARS NOTHING HAS CHANGED. I CALLED FORD COMPANYAND WAS TOLD TO TAKE IT TO FORD DEALER. (I TOOK IT TO FORD DEALERSHIP AND TOLD THEM WHAT THE PROBLEM WAS. I ALSO STATED THAT IT STOPS SHIFTING INTO 4TH GEAR AND WILL NOT SHIFT UP IF I HAVE TO ACCELERATE QUICKLY. THE DEALER INFO: FORD BREDEMANN 2038 WAUKEGAN ROAD GLENVIEW, IL 60025 (847) 510-5585). I LEFT THE CAR FOR ABOUT A WEEK AND WHEN I CAME TO PICK IT UP I WAS TOLD THAT ENGINE AND TRANSMISSION WERE ON GOOD CONDITION. THERE ARE SOME THINGS THAT NEEDED TO BE CHANGED LIKE TIRES..ETC.. HOWEVER, I HAVE HAD INSTANCES ON THE ROAD WHERE I ALMOST COULD HAVE ENDED UP KILLED JUST BECAUSE THE CAR WONT ACCELERATE. IT HAPPENED TO ME ABOUT TWO WEEKS AGO. 2ND PROBLEM IS STEERING WHEEL. IT IS SO STIFF THAT ITS HARD TO TURN IT LEFT AND RIGHT. I FEEL LIKE IT IS SO UNSAFE FOR ME TO DRIVE THIS CAR..NOT JUST UNSAFE FOR ME BUT FOR OTHER DRIVERS ON THE ROAD WAS WELL. *TR

NHTSA #: 10437315
mediumENGINE AND ENGINE COOLING
Filed: Apr 2010

TL* THE CONTACT OWNS A 2006 FORD FOCUS. THE CONTACT STARTED THE IGNITION AND THERE WAS A RATTLING NOISE. THE VEHICLE WAS TAKEN TO AN INDEPENDENT MECHANIC WHERE THE TECHNICIAN DETECTED TWO OF THE FOUR ENGINE MOUNTS WERE BROKEN. THE MECHANIC REPAIRED THE VEHICLE AND STATED THE FAILURE SHOULD NOT OCCURRED ON A FOUR YEAR OLD VEHICLE. THE FAILURE MILEAGE AND CURRENT MILEAGES WERE 131,000.

NHTSA #: 10326461
mediumENGINE AND ENGINE COOLING
Filed: Dec 2008

2006 FOR FOCUS 2.0 I-4 BLEW OUT SPARK PLUG OUT OF THE HEAD N WITH IGNITION COIL. END RESULT FINDING THAT THE CAR HAD THE WRONG SPARK PLUGS FROM THE FACTORY. AND FORD WONT FIX THEIR MISTAKE. THE CAR IS UNDER WARRANTY. *TR

NHTSA #: 10253123
mediumENGINE AND ENGINE COOLING
FireFiled: Apr 2008

ON THE 19TH OF APRIL, MY VEHICLE WAS PERFORMING NORMALLY. ON THE 20TH OF APRIL, THE VEHICLE WAS UNABLE TO ATTAIN NORMAL DRIVING SPEEDS; TOP SPEED WAS AROUND 20 MPH. AS A RESULT, WE CHOSE TO RETURN HOME IMMEDIATELY AND TO BRING THE VEHICLE TO THE DEALERSHIP THE NEXT DAY. ON THE 21ST, AROUND 10:15 A.M., I BEGAN TO DRIVE THE VEHICLE TO THE DEALERSHIP. HOWEVER, AFTER APPROXIMATELY 1.5 MILES, THE ENGINE BEGAN CUTTING OUT COMPLETELY AND THERE WAS A STRANGE ODOR. I GOT THE VEHICLE RESTARTED AND PULLED INTO AN ADJACENT PARKING LOT. I PARKED THE VEHICLE AND SHUT IT OFF. I FOUND A NEARBY STORE FROM WHICH I COULD CALL HOME. WHEN I STEPPED BACK OUTSIDE I WAS UNABLE TO SEE THE VEHICLE DUE TO SMOKE. I RETURNED TO THE STORE AND IMMEDIATELY CALLED 911. BY THE TIME I STEPPED BACK OUTSIDE, THERE WERE VISIBLE FLAMES. POLICE AND FIRE RESPONDED, BUT THE VEHICLE WAS A COMPLETE LOSS. *TR

NHTSA #: 10225441
mediumENGINE AND ENGINE COOLING
Filed: Mar 2007

I'VE HAD MY 2006 FOCUS ST FOR ABOUT A YEAR NOW. SINCE I BOUGHT MY CAR I HAVE HAD TO HAVE 3 DIFFERENT ENGINES PUT IN IT. THE ORIGINAL MOTOR THREW A PISTON ROD DOWN THE BOTTOM OF MY ENGINE AND OUT. THEY SAID IT WAS POOR CASTING ON THE CRANKSHAFT. THIS WAS AT ABOUT 4,000 MILES. THEN AT ABOUT 15,000 MILES IT DID THE SAME THING ONLY THIS TIME I CAUGHT IT BEFORE IT BLEW. NEEDLESS TO SAY I HAD TO HAVE A NEW ENGINE ...AGAIN. WHAT HAPPENED IS MY ROD BEARINGS WENT OUT WHICH IS MOST LIKELY WHAT HAPPENED THE FIRST TIME, CAUSING MY ENGINE TO COMPLETELY THROW A PISTON ROD. NOW I AM ON MY 3RD ENGINE AND HOPING THAT THIS ONE STICKS. THE MECHANICS ARE VERY PUZZLED WHY THIS IS HAPPENING. THEY HAVE RUN ALL THE DIAGNOSTICS TO PROVE I HAVEN'T BEEN RACING AND I GET REGULAR OIL CHANGES THROUGH THE DEALERSHIP. FORD IS TRYING TO GET TO THE BOTTOM OF IT. GOOD NEWS IS 2 MORE TIMES IT'S A LEMON. BAD NEWS IS I HAVE HAD TO DEAL WITH MISSED TIME AT WORK AND THE INCONVENIENCE OF IT ALL. BEWARE BUT, THIS DOESN'T SEEM TO BE A REGULAR OCCURRENCE AMONG FOCUS OWNERS. *JB

NHTSA #: 10183862
mediumENGINE AND ENGINE COOLING
Filed: Jun 2006

DT*: THE CONTACT STATED THAT THE VEHICLE'S VENTING SYSTEM BLEW WHITE FLAKES AND DUST INSIDE THE VEHICLE WHEN THE HEATER OR AIR CONDITIONING UNIT WAS ACTIVATED. THE FIRST TIME THE INCIDENT OCCURRED THE HEATER WAS ON. THE VEHICLE WAS TAKEN TO THE DEALER WHO CLEANED INSIDE THE VENTING SYSTEM BUT COULD NOT FIND ANY PROBLEM WITH THE VEHICLE. THE VEHICLE WAS TAKEN TO THE DEALER SEVERAL TIMES BECAUSE WHITE FLAKES CONTINUED BLOWING THROUGH THE VENTS. THE DEALER DETERMINED THAT A CLEANING AGENT THAT MAY HAVE BEEN USED TO CLEAN METAL KNOWN AS SOLDERING FLUX MAY BE THE CAUSE OF WHITE FLAKES COMING FROM THE VENTS. THE EVAPORATOR COIL HOUSING WAS REPLACED ON 04/07/06. THE EVAPORATOR COIL HOUSING WAS CLEANED ON 04/21/06. THE VEHICLE VENTING SYSTEM WAS CLEANED AGAIN ON 05/23/06, BUT THE PROBLEM PERSISTED. THE CONTACT EXPRESSED CONCERN ABOUT THIS CAUSING A RESPIRATORY PROBLEM.

NHTSA #: 10160954

Other 2006 Ford Focus Issues